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	<title>Allied Reliability Knowledge Center &#187; Asset Health</title>
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		<title>Reliability Centered Lubrication &#8211; A Success Story</title>
		<link>http://alliedreliabilityblog.com/2012/03/reliability-centered-lubrication-a-success-story/</link>
		<comments>http://alliedreliabilityblog.com/2012/03/reliability-centered-lubrication-a-success-story/#comments</comments>
		<pubDate>Thu, 01 Mar 2012 20:25:15 +0000</pubDate>
		<dc:creator>Allied</dc:creator>
				<category><![CDATA[Articles]]></category>
		<category><![CDATA[Asset Health]]></category>
		<category><![CDATA[Condition Based Monitoring]]></category>
		<category><![CDATA[Maintenance]]></category>
		<category><![CDATA[Predictive Maintenance]]></category>
		<category><![CDATA[Preventitive Maintenance]]></category>
		<category><![CDATA[Reliability]]></category>
		<category><![CDATA[Reliability Centered Maintenance]]></category>
		<category><![CDATA[efficiency]]></category>
		<category><![CDATA[failure modes]]></category>
		<category><![CDATA[Leadership]]></category>
		<category><![CDATA[lubrication]]></category>
		<category><![CDATA[machine parts]]></category>
		<category><![CDATA[maintenance supervision]]></category>
		<category><![CDATA[oil analysis]]></category>
		<category><![CDATA[planning and scheduling]]></category>
		<category><![CDATA[strategy]]></category>

		<guid isPermaLink="false">http://alliedreliabilityblog.com/?p=334</guid>
		<description><![CDATA[By Stacy Heston, CLS, PMP, CMRP, OMA, Lubrication Subject Matter Expert, Allied Reliability Inc. Lubrication practices are often overlooked as a potential time and money saver for a plant.  However Cargill Charlotte has found that by optimizing their lubrication task intervals, utilizing specific grease volumes, and implementing an oil analysis program, the overall reliability of [...]]]></description>
			<content:encoded><![CDATA[<p></p><h2 style="text-align: center;">By Stacy Heston, CLS, PMP, CMRP, OMA, Lubrication Subject Matter Expert, Allied Reliability Inc.</h2>
<p><a href="http://www.alliedreliability.com/lubrication_design.asp" target="_blank">Lubrication</a> practices are often overlooked as a potential time and money saver for a plant.  However <a href="http://www.cargill.com/" target="_blank">Cargill Charlotte </a>has found that by optimizing their lubrication task intervals, utilizing specific grease volumes, and implementing an <a href="http://www.alliedreliability.com/oil_analysis.asp" target="_blank">oil analysis program</a>, the overall reliability of their manufacturing process, as well as, the healthy status of their lubricated components has increased.<br />
In 2009, <a href="http://www.alliedreliability.com/default.asp" target="_blank">Allied Reliability </a>performed a <a href="http://www.alliedreliability.com/lubrication_design.asp" target="_blank">Reliability Centered Lubrication Current State Analysis </a>at the site to determine the state of the lubrication program.  Through the assignment of a score to different lubrication activity and practices, the site’s lubrication program was benchmarked on several parameters including program documentation, management structure and practices, storage and handling, etc.  By assigning a score, the benchmarking activity becomes more objective and less subjective allowing for a definitive path forward.<br />
When<a href="http://www.alliedreliability.com/default.asp" target="_blank"> Allied Reliability </a>arrived on site, “the site had run amuck with lubricants everywhere, it was all about the flavor of the month…” where lubrication was concerned, and “no structure existed for the scheduling of lubrication tasks,” says Andy Nolan.  As a result of the Current State Analysis, it was determined that a <a href="http://www.alliedreliability.com/lubrication_design.asp" target="_blank">RCL</a> walk down was needed to bring the site up to speed with industry best practices for lubrication.<br />
Shortly after the Current State Analysis, <a href="http://www.alliedreliability.com/default.asp" target="_blank">Allied Reliability </a>began the development of a <a href="http://www.alliedreliability.com/lubrication_design.asp" target="_blank">Reliability Centered Lubrication Program </a>at the site.  The program design began with a full walk down of all lubricated components on site.  During the walk down phase, all data pertinent to the development of lubrication specifications, interval calculations, and lubricant quantity calculations is gathered.  This phase sets the stage for the remaining program design as the accuracy and content of this data is the core to a strong program.<br />
During the <a href="http://www.alliedreliability.com/lubrication_design.asp" target="_blank">walk down</a>, opportunities for optimizing intervals are identified as well as opportunities for optimizing the lubricant list.  Optimization does not always mean an increase in intervals or a decrease in the number of lubricants on site, rather it is the assignment of calculated intervals that are specific to the component and takes into account the specific operating conditions the component is exposed to.  Essentially, the same bearing may be exposed to wash down practices and heavy debris requiring an increased interval, such as 30 days to account for these environmental exposures.  However, the same type of bearing operating at the same speed with limited exposure to moisture and no exposure to debris may have an interval of 360 days.  This deviation in intervals means that the bearing with the more aggressive environment and operating conditions receives the more aggressive treatment.<br />
When the Charlotte site began the implementation phase of their <a href="http://www.alliedreliability.com/lubrication_design.asp" target="_blank">RCL</a> program, the lubricated components were in poor health.  Approximately 60% of the oil lubricated assets were considered to be in the red, or in a state that did not meet industry best practices for contamination control, operating temperature, etc.  Within three months, the percentage decreased to approximately 40%.  By the end of 2010, 100% of all oil lubricated assets had achieved a green status.</p>
<p><a href="http://alliedreliabilityblog.com/wp-content/uploads/2012/03/71056175.jpg"><img class="alignleft size-medium wp-image-335" title="71056175" src="http://alliedreliabilityblog.com/wp-content/uploads/2012/03/71056175-300x198.jpg" alt="" width="300" height="198" /></a></p>
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<p>Components were easily converted from a red state to a green state through the implementation of <a href="http://www.alliedreliability.com/oil_analysis.asp" target="_blank">oil analysis</a>, off line filtration, and monthly inspections. <a href="http://www.alliedreliability.com/oil_analysis.asp" target="_blank"> Oil analysis </a>aids in the identification of in use lubricants that required filtration to clean up solid contaminates, needed refreshing due to changes in additive levels and lubricant properties, or need complete replacement.<br />
Previous to the implementation phase, the site utilized a time based oil change methods, had a multitude of lubricants with no specific requirements for each component, utilized screen breathers, and had no structure for the inclusion of filtration.  Lubricants were stored in drums and in areas that did not provide a clean, temperature controlled atmosphere.  The overall program lacked structure with regards to regrease intervals and amounts, as well as, oil analysis and oil change intervals.<br />
The implementation phase of the <a href="http://www.alliedreliability.com/lubrication_design.asp" target="_blank">RCL Program Design </a>included recommendations for component modification with items such as desiccant breathers, quick connect couplings, level gauges, and sample valves.  These modifications provide multiple benefits for the lubrication program as well as the plant operating structure as a whole.  Level gauges and sample valves allow lube technicians to perform level checks and sample collection tasks with the machine running.  Without these modifications, the machine and possibly the product line would need to be down for the completion of these tasks.  It also saves time from a labor perspective.  A dipstick level indicator involves several steps to determine the level and exposes the lubricant to the possibility of contamination, where as a visual level gauge is nothing more than a quick peek then walk on to the next component.<br />
The Charlotte site followed some very basic steps to manage the program implementation starting with the incorporation of <a href="http://en.wikipedia.org/wiki/Desiccant" target="_blank">desiccant</a> breathers and other types.  After some experimentation with different types of breathers, there was an eventual shift to the use of trap and hybrid breathers based on the components size and location within the plant.  Of all the modifications, breathers are the least evasive to install, and limits the amount of debris able to enter the sump down to 3µ in size.<br />
The second step included the conversion of mineral based oils to synthetic based oils in the smaller sump components.  Using the current practice of 6 or 12 month oil drains, each sump was converted during the next scheduled oil drain task.  At that time, new intervals of 12 or 18 month were implemented for each sump.  This step applies only to sumps that are too small for oil sampling.<br />
The third step was the implementation of<a href="http://www.alliedreliability.com/oil_analysis.asp" target="_blank"> oil sampling practices </a>on sumps within the 4 to 22 gallon range.  This implementation allowed for the extension of oil drains through the monitoring of the lubricant health.  Unlike the second step, these components were not immediately converted to a synthetic oil.  Rather the current lubricant was monitored and cared for until such time the <a href="http://www.alliedreliability.com/oil_analysis.asp" target="_blank">oil analysis </a>results showed a break down in the lubricant properties.  Once the lubricant properties began to degrade, an oil change with conversion to a synthetic occurred.  This maximized the life of the lubricant that was in service before change over without harm to the component.<br />
*During lubricant drains, additional modifications were implemented while the sumps were empty such as the installation of level gauges, quick connects, and sample valves.<br />
Once the oil lubricated components had been addressed, the fourth step was implemented.  The fourth step was the mass implementation of the grease lubrication routes that were developed based on the walk down phase.  These routes were provided in an electronic format which is downloadable to a pda, or other handheld device.  The routes were grouped together based on location within the plant, lubricant required, and interval.  The interval and re-grease volumes are calculated using gathered data to ensure the right amount of lubricant is delivered at the right time.<br />
At the onset of the <a href="http://www.alliedreliability.com/lubrication_design.asp" target="_blank">RCL design</a>, this location had 1 overworked lubrication technician.  Now, they have 1 lubrication technician who is able to complete all required tasks within a timely manner because a solid program structure has been implemented to address all aspects of lubrication.  Task intervals have been optimized to ensure over and under lubrication is not an issue, and oil drain intervals have been extended.  Additionally, lubrication related failures have decreased allowing focus to shift from putting out fires to maintaining the current state.<br />
“We now have a set program that anyone can follow with component state data being collected regularly to ensure appropriate actions are taken to avoid lubricant and component failure.  We have structure and focus.”</p>
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		<title>Online Motor Circuit Analysis Testing for Mechanical Defects</title>
		<link>http://alliedreliabilityblog.com/2011/12/online-motor-circuit-analysis-testing-for-mechanical-defects/</link>
		<comments>http://alliedreliabilityblog.com/2011/12/online-motor-circuit-analysis-testing-for-mechanical-defects/#comments</comments>
		<pubDate>Thu, 22 Dec 2011 17:27:54 +0000</pubDate>
		<dc:creator>Allied</dc:creator>
				<category><![CDATA[Asset Health]]></category>
		<category><![CDATA[Case Study]]></category>
		<category><![CDATA[Condition Based Monitoring]]></category>
		<category><![CDATA[Maintenance]]></category>
		<category><![CDATA[Predictive Maintenance]]></category>
		<category><![CDATA[Preventitive Maintenance]]></category>
		<category><![CDATA[Reliability]]></category>
		<category><![CDATA[machine parts]]></category>
		<category><![CDATA[motor circut analysis]]></category>
		<category><![CDATA[pinion]]></category>
		<category><![CDATA[planning and scheduling]]></category>
		<category><![CDATA[shaft misalignment]]></category>
		<category><![CDATA[thermography]]></category>
		<category><![CDATA[ultrasonic]]></category>
		<category><![CDATA[vibration]]></category>
		<category><![CDATA[vibration analysis]]></category>

		<guid isPermaLink="false">http://alliedreliabilityblog.com/?p=294</guid>
		<description><![CDATA[By: T.J. Garten, IR/MCA Specialist Bean Conditioner – Horizontal Rotary Vessel Motor:        TECO-Westinghouse          75 HP                     1775 RPM Gearbox:     Falk 2120Y3-1                    Ratio: 70.09 Pinion:       19 tooth Synopsis The Bean Conditioner is a rotary vessel used to condition soy beans prior to transportation to flaking equipment. This particular vessel rotates on a slight uphill axis and is [...]]]></description>
			<content:encoded><![CDATA[<p></p><h2 style="text-align: center;"><span style="color: #000000;">By: T.J. Garten, <a href="http://www.alliedreliability.com/infrared.asp" target="_blank">IR</a>/<a href="http://www.alliedreliability.com/motor.asp" target="_blank">MCA</a> Specialist</span></h2>
<h2><span style="color: #000000;"><strong>Bean Conditioner – Horizontal Rotary Vessel</strong></span></h2>
<div style="padding-left: 30px;"><span style="color: #000000;">Motor:        TECO-Westinghouse          75 HP                     1775 RPM</span></div>
<div style="padding-left: 30px;"><span style="color: #000000;">Gearbox:     Falk 2120Y3-1                    Ratio: 70.09</span></div>
<div style="padding-left: 30px;"><span style="color: #000000;">Pinion:       19 tooth</span></div>
<h2><span style="color: #000000;"><em>Synopsis</em></span></h2>
<div style="padding-left: 30px;"><span style="color: #000000; font-size: small;"><span style="font-size: small;">The Bean Conditioner is a rotary vessel used to condition soy beans prior to transportation to flaking equipment. This particular vessel rotates on a slight uphill axis and is driven by a 75 HP 1775 RPM motor coupled to a 70.09 reduction gearbox and a 19 tooth <a href="http://en.wikipedia.org/wiki/Pinion" target="_blank">pinion</a>. The vessel has a bull gear assembly that the 19 tooth pinion drives. During the months leading up to the repair, a visible shaking of the feed screw platform was noted during every revolution of the vessel. In addition, the pedestals for the pillow block bearings for the pinion gear shaft could be seen bending inward during the revolution. This bending motion coincided with the vibration of the feeder screw platform. Due to guarding of the pinion assembly, <a href="http://www.alliedreliability.com/vibration_analysis.asp" target="_blank">vibration</a> data collection was not practical and remote provisions had not been installed. </span></span></div>
<h2><span style="color: #000000;"><em>Fault</em></span></h2>
<div style="padding-left: 30px;"><span style="color: #000000; font-size: small;"><span style="font-size: small;">During the quarterly <a href="http://www.alliedreliability.com/motor.asp" target="_blank">Motor Circuit Analysis (MCA)</a> online data collection, the July 6, 2009 data showed a marked increase in the dB for the peak associated with the 19 tooth pinion. Identification of the anomaly peak in the <a href="http://en.wikipedia.org/wiki/Frequency_modulation#Demodulation" target="_blank">demodulation spectrum</a> was accomplished by identifying the motor turning speed (TS), calculating the gearbox output shaft TS, and then multiplying that TS by the number of teeth on the pinion gear. This calculation gives the RPM of the pinion gear mesh, which then needs to be converted into hertz (divide the RPM of the pinion gear mesh by 60) to locate the peak in the demodulation spectrum. (See Figure 1.) </span></span></div>
<div style="padding-left: 60px;"><span style="color: #000000;"><span style="font-size: small;"><span style="font-size: small;">TS</span></span><span style="font-size: xx-small;"><span style="font-size: xx-small;">Motor </span></span><span style="font-size: small;"><span style="font-size: small;">/ Gearbox Ratio = TS</span></span><span style="font-size: xx-small;"><span style="font-size: xx-small;">GearboxOut </span></span></span></div>
<div style="padding-left: 60px;"><span style="color: #000000;"><span style="font-size: small;"><span style="font-size: small;">(TS</span></span><span style="font-size: xx-small;"><span style="font-size: xx-small;">GearboxOut </span></span><span style="font-size: small;"><span style="font-size: small;">* Number of Teeth on Pinion) / 60 = Pinion Frequency </span></span></span></div>
<div style="padding-left: 30px;"><span style="color: #000000;">Using the July 6, 2009 data:</span></div>
<div><span style="color: #000000; font-size: small;"><span style="font-size: small;"> </span></span></div>
<div style="padding-left: 60px;"><span style="color: #000000;">1785 / 70.09 = 25.47 RPM</span></div>
<div style="padding-left: 60px;"><span style="color: #000000; font-size: small;"><span style="font-size: small;">25.47 * 19 = 483.93 RPM / 60 = 8.07 Hz </span></span></div>
<div style="padding-left: 30px;"><span style="color: #000000;"><em><span style="font-size: small;"><span style="font-size: small;">Note: Slight deviations (less than 1%) may occur due to variations in the turning speed of the motor. </span></span></em></span></div>
<div><em><span style="color: #1f487c; font-size: small;"><span style="color: #1f487c; font-size: small;"> </span></span></em><span style="color: #1f487c; font-family: Times New Roman,Times New Roman; font-size: small;"><span style="color: #1f487c; font-family: Times New Roman,Times New Roman; font-size: small;"><span style="color: #1f487c; font-family: Times New Roman,Times New Roman; font-size: small;"> </span></span></span></div>
<div style="padding-left: 30px;">Historically, the 8.09 Hz baseline peak operated in a 1.1 to 1.5 dB range, depending on loading. From the initial alarm trip until the next scheduled shutdown during September 2010, the dB peak increased to 4.81 dB, with one data capture of over 5.1 dB in April 2010. (See Figure 2.) During this time, the visible shaking of the feed screw platform increased from minor to severe.</div>
<div style="padding-left: 30px;"><a href="http://www.alliedreliability.com/visual_inspections.asp" target="_blank">Visual inspection </a>of the pinion shaft assembly noted broken welds on the pedestals for the pillow blocks (Figure 4), as well as inward bending during every rotation of the vessel. The flexible coupling <span style="color: #000000; font-size: small;"><span style="font-size: small;">that joined the gearbox output shaft with the pinion gear shaft also exhibited wrap flex heating, as determined through <a href="http://www.alliedreliability.com/infrared.asp" target="_blank">thermography scans</a>, and appeared to have visible angular misalignment.</span></span></div>
<h2>Summary of Action</h2>
<div style="padding-left: 30px;">During discussions with the site, it was determined that before the 2009 shutdown, a trunnion pillow block bearing had failed. During the repair of this bearing, the vessel height had to be adjusted due to a different roller height and consequential opening of the pinion gear-to-bull gear mating. This correction was made at the pinion shaft utilizing dial indicators. No testing had been performed after this repair due to plant outages and scheduling concerns. The first testing time was a period of four months after the repair.</div>
<div style="padding-left: 60px;">During the 2010 shutdown, the contracted mechanical crew noticed the following:</div>
<div style="padding-left: 90px;">• The pinion shaft was lower than the gearbox output shaft.</div>
<div style="padding-left: 90px;">• There was a high spot on the vessel bull gear.</div>
<div style="padding-left: 90px;">• The clearance between the pinion gear and the bull gear was too small.</div>
<div style="padding-left: 90px;">• There were increased levels of mating rub on the pinion gear teeth.</div>
<div style="padding-left: 60px;">The shaft alignment was corrected, the pinion gear was flipped to change the wear pattern on the teeth, the pinion-to-bull gear clearance was changed to account for the high spot on the vessel, and the pedestals were welded.</div>
<div style="padding-left: 60px;">During the subsequent site visit, the vibration of the feed screw platform was no longer present. In addition, the <a href="http://www.alliedreliability.com/motor.asp" target="_blank">MCA</a> online demodulation data showed a return to normal dB ranges (Figure 5).</div>
<div style="padding-left: 60px;"><span style="color: #000000;">However, over the next year, the same pattern began to develop again. The welds had broken again and required additional welding during the 2011 shutdown.</span></div>
<h2><span style="color: #000000;"><em>Supporting Data</em></span></h2>
<div id="attachment_296" class="wp-caption alignleft" style="width: 300px">
	<a href="http://alliedreliabilityblog.com/wp-content/uploads/2011/12/Case-Study_Online-MCA-Testing-for-Mechanical-Defects-1.jpg"><span style="color: #000000;"><img class="size-medium wp-image-296" title="Case Study_Online MCA Testing for Mechanical Defects 1" src="http://alliedreliabilityblog.com/wp-content/uploads/2011/12/Case-Study_Online-MCA-Testing-for-Mechanical-Defects-1-300x75.jpg" alt="" width="300" height="75" /></span></a>
	<p class="wp-caption-text">Figure 1: Pre-repair Demodulation Spectrum</p>
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<div id="attachment_297" class="wp-caption alignleft" style="width: 300px">
	<a href="http://alliedreliabilityblog.com/wp-content/uploads/2011/12/Case-Study_Online-MCA-Testing-for-Mechanical-Defects-2.jpg"><img class="size-medium wp-image-297" title="Case Study_Online MCA Testing for Mechanical Defects 2" src="http://alliedreliabilityblog.com/wp-content/uploads/2011/12/Case-Study_Online-MCA-Testing-for-Mechanical-Defects-2-300x185.jpg" alt="" width="300" height="185" /></a>
	<p class="wp-caption-text">Figure 2: Pre-repair Historical Data</p>
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<div id="attachment_298" class="wp-caption alignleft" style="width: 300px">
	<a href="http://alliedreliabilityblog.com/wp-content/uploads/2011/12/Case-Study_Online-MCA-Testing-for-Mechanical-Defects-3.jpg"><img class="size-medium wp-image-298" title="Case Study_Online MCA Testing for Mechanical Defects 3" src="http://alliedreliabilityblog.com/wp-content/uploads/2011/12/Case-Study_Online-MCA-Testing-for-Mechanical-Defects-3-300x225.jpg" alt="" width="300" height="225" /></a>
	<p class="wp-caption-text">Figure 3: Pinion Wear</p>
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<div id="attachment_301" class="wp-caption alignleft" style="width: 300px">
	<a href="http://alliedreliabilityblog.com/wp-content/uploads/2011/12/Case-Study_Online-MCA-Testing-for-Mechanical-Defects-451.jpg"><img class="size-medium wp-image-301" title="Case Study_Online MCA Testing for Mechanical Defects 45" src="http://alliedreliabilityblog.com/wp-content/uploads/2011/12/Case-Study_Online-MCA-Testing-for-Mechanical-Defects-451-300x142.jpg" alt="" width="300" height="142" /></a>
	<p class="wp-caption-text">Figure 4: Broken Welds on Pinion Gear Pillow Block Pedestal</p>
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<div id="attachment_302" class="wp-caption alignnone" style="width: 188px">
	<a href="http://alliedreliabilityblog.com/wp-content/uploads/2011/12/Case-Study_Online-MCA-Testing-for-Mechanical-Defects-6.jpg"><img class="size-medium wp-image-302" title="Case Study_Online MCA Testing for Mechanical Defects 6" src="http://alliedreliabilityblog.com/wp-content/uploads/2011/12/Case-Study_Online-MCA-Testing-for-Mechanical-Defects-6-188x300.jpg" alt="" width="188" height="300" /></a>
	<p class="wp-caption-text">Figure 5: Post-repair Demodulation Data</p>
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<h2>Conclusion</h2>
<p style="padding-left: 30px;">The corrective action taken during the repair of the failed trunnion bearing resulted in an altered elevation of the rotary vessel. The attempts to adjust for this were inadequate and resulted in a changed mating pattern between the pinion gear and bull gear assemblies. Over time, the increased impacting caused the pinion shaft to deflect, breaking the welds on the pedestals. This deflection also caused an angular misalignment between the pinion shaft and the gearbox output shaft. The level of misalignment may also have been affected by utilizing dial indicators for precision shaft alignment rather than the on-site laser alignment equipment. As the trunnion rollers wear, the clearance between the pinion gear and bull gear’s high spot decreases, resulting in increased shaft deflection. The increased shaft deflection results in transmitted vibration to the feed screw platform and torsional stress on the gearbox output coupling.Future corrections need to take into account all clearances and their effect on correlating components. Monitoring of adjusted components should be within days of adjustments and load changes. Installation of remote accelerometers on the pinion gear shaft pillow blocks would allow for quicker analysis of shaft misalignment, bearing condition, and pinion gear mesh frequencies.</p>
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		<title>Radio Frequency Interference on Commtest VBx Series Data Collectors From Improperly Grounded Equipment</title>
		<link>http://alliedreliabilityblog.com/2011/10/radio-frequency-interference-on-commtest-vbx-series-data-collectors-from-improperly-grounded-equipment/</link>
		<comments>http://alliedreliabilityblog.com/2011/10/radio-frequency-interference-on-commtest-vbx-series-data-collectors-from-improperly-grounded-equipment/#comments</comments>
		<pubDate>Tue, 25 Oct 2011 15:02:02 +0000</pubDate>
		<dc:creator>Allied</dc:creator>
				<category><![CDATA[Asset Health]]></category>
		<category><![CDATA[Condition Based Monitoring]]></category>
		<category><![CDATA[Predictive Maintenance]]></category>
		<category><![CDATA[Preventitive Maintenance]]></category>
		<category><![CDATA[vibration]]></category>
		<category><![CDATA[vibration analysis]]></category>

		<guid isPermaLink="false">http://alliedreliabilityblog.com/?p=282</guid>
		<description><![CDATA[Don&#8217;t Let the title fool you, this is a great and very short case study!  Allied Reliability SME Aubrey Green examines a dilemma at a salt evaporation plant in upper NY.  Read it for yourself here: Radio Frequency Interference on Commtest VBx Series Data Collectors from Improperly Grounded Equipment]]></description>
			<content:encoded><![CDATA[<p></p><p>Don&#8217;t Let the title fool you, this is a great and very short case study!  Allied Reliability SME Aubrey Green examines a dilemma at a salt evaporation plant in upper NY.  Read it for yourself here:</p>
<p><a title="radio frequency improperly grounded equipment" href="http://www.alliedreliability.com/pdf/Case-Study-Radio-Frequency-Interference.pdf" target="_blank">Radio Frequency Interference on Commtest VBx Series Data Collectors from Improperly Grounded Equipment</a></p>
]]></content:encoded>
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		<title>Maintenance Planning is Too Hard in my Workplace</title>
		<link>http://alliedreliabilityblog.com/2011/08/maintenance-planning-is-too-hard-in-my-workplace/</link>
		<comments>http://alliedreliabilityblog.com/2011/08/maintenance-planning-is-too-hard-in-my-workplace/#comments</comments>
		<pubDate>Mon, 01 Aug 2011 19:43:43 +0000</pubDate>
		<dc:creator>Allied</dc:creator>
				<category><![CDATA[Articles]]></category>
		<category><![CDATA[Asset Health]]></category>
		<category><![CDATA[Maintenance]]></category>
		<category><![CDATA[Leadership]]></category>
		<category><![CDATA[maintenance supervision]]></category>
		<category><![CDATA[planning and scheduling]]></category>
		<category><![CDATA[strategy]]></category>

		<guid isPermaLink="false">http://alliedreliabilityblog.com/?p=263</guid>
		<description><![CDATA[Ricky Smith SME for GPAllied examines the common roadblocks and excuses surrounding maintenance planning.  Ricky will walk you through steps that can take you from where you are to &#8216;World Class&#8217;.  Article as printed in the July issue of Asset Management and Maintenance Journal.  Read it for yourself here: Maintenance Planning is Too Hard in [...]]]></description>
			<content:encoded><![CDATA[<p></p><p>Ricky Smith SME for GP<em>Allied </em>examines the common roadblocks and excuses surrounding maintenance planning.  Ricky will walk you through steps that can take you from where you are to &#8216;World Class&#8217;.  Article as printed in the July issue of Asset Management and Maintenance Journal.  Read it for yourself here:</p>
<p><a title="Maintenance Planning is too Hard" href="http://www.alliedreliability.com/pdf/ammj%20july%20ricky%20smith%20article%20w%20cover.pdf" target="_blank">Maintenance Planning is Too Hard in my Workplace</a></p>
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		<slash:comments>2</slash:comments>
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		<title>Clean, Green &amp; Reliable</title>
		<link>http://alliedreliabilityblog.com/2011/07/clean-green-reliable/</link>
		<comments>http://alliedreliabilityblog.com/2011/07/clean-green-reliable/#comments</comments>
		<pubDate>Tue, 26 Jul 2011 12:53:35 +0000</pubDate>
		<dc:creator>Allied</dc:creator>
				<category><![CDATA[Articles]]></category>
		<category><![CDATA[Asset Health]]></category>
		<category><![CDATA[Reliability Centered Maintenance]]></category>
		<category><![CDATA[efficiency]]></category>
		<category><![CDATA[electrical]]></category>
		<category><![CDATA[green technology]]></category>

		<guid isPermaLink="false">http://alliedreliabilityblog.com/?p=259</guid>
		<description><![CDATA[GPAllied Subject Matter Experts Chris Colson and Doug Plucknette dive into how equipment reliability delivers low-cost, energy-efficient assets at plants around the world.  As published in the July edition of Uptime Magazine.  Read it for yourself here: Clean, Green &#38; Reliable]]></description>
			<content:encoded><![CDATA[<p></p><p>GP<em>Allied</em> Subject Matter Experts Chris Colson and Doug Plucknette dive into how equipment reliability delivers low-cost, energy-efficient assets at plants around the world.  As published in the July edition of Uptime Magazine.  Read it for yourself here:</p>
<p><a title="clean green and reliable" href="http://www.alliedreliability.com/pdf/clean_green_and_reliable_hi_res.pdf" target="_blank">Clean, Green &amp; Reliable</a></p>
]]></content:encoded>
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		<title>Things to do and think about 2011- DATA</title>
		<link>http://alliedreliabilityblog.com/2011/05/things-to-do-and-think-about-2011-data/</link>
		<comments>http://alliedreliabilityblog.com/2011/05/things-to-do-and-think-about-2011-data/#comments</comments>
		<pubDate>Thu, 05 May 2011 20:23:30 +0000</pubDate>
		<dc:creator>Allied</dc:creator>
				<category><![CDATA[Articles]]></category>
		<category><![CDATA[Asset Health]]></category>
		<category><![CDATA[Maintenance]]></category>
		<category><![CDATA[Predictive Maintenance]]></category>
		<category><![CDATA[data management]]></category>
		<category><![CDATA[data streamlining]]></category>

		<guid isPermaLink="false">http://alliedreliabilityblog.com/?p=230</guid>
		<description><![CDATA[Every year Reliabilityweb publishes an eBook on top tips, opinions and viewpoints from industry thought leaders and subject matter experts from around the world.  Stacy Heston, Subject Matter Expert in Lubrication was featured in this 2011 edition with her tips on data entry.  Read it for yourself here: Things to do and think about 2011- DATA]]></description>
			<content:encoded><![CDATA[<p></p><p>Every year Reliabilityweb publishes an eBook on top tips, opinions and viewpoints from industry thought leaders and subject matter experts from around the world.  Stacy Heston, Subject Matter Expert in Lubrication was featured in this 2011 edition with her tips on data entry.  Read it for yourself here:</p>
<p><a title="things to do- data" href="http://www.alliedreliability.com/pdf/ThingsToThinkAbout2011_(Heston%20Data).pdf" target="_blank">Things to do and think about 2011- DATA</a></p>
]]></content:encoded>
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		<title>Article: &#8220;Nourishing Reliability and Healthy Assets&#8221;</title>
		<link>http://alliedreliabilityblog.com/2010/05/article-nourishing-reliability-and-healthy-assets/</link>
		<comments>http://alliedreliabilityblog.com/2010/05/article-nourishing-reliability-and-healthy-assets/#comments</comments>
		<pubDate>Fri, 07 May 2010 17:28:41 +0000</pubDate>
		<dc:creator>Allied</dc:creator>
				<category><![CDATA[Articles]]></category>
		<category><![CDATA[Asset Health]]></category>
		<category><![CDATA[Case Study]]></category>
		<category><![CDATA[Condition Based Monitoring]]></category>
		<category><![CDATA[Featured]]></category>
		<category><![CDATA[Reliability]]></category>
		<category><![CDATA[machine parts]]></category>
		<category><![CDATA[motor circut analysis]]></category>
		<category><![CDATA[oil analysis]]></category>
		<category><![CDATA[ultrasonic]]></category>
		<category><![CDATA[vibration analysis]]></category>

		<guid isPermaLink="false">http://alliedreliabilityblog.com/?p=109</guid>
		<description><![CDATA[John Schultz, with co-authors Rick Baldridge and Tim Goshert, wrote an artilce on Reliability and Healthy Assets. Read it for yourself here: &#8220;Nourishing Reliability and Healthy Assets&#8221;]]></description>
			<content:encoded><![CDATA[<p></p><p style="line-height: 13.15pt;"><span style="font-family: 'Georgia','serif'; font-size: 9pt;">John Schultz, with co-authors Rick Baldridge and Tim Goshert, wrote an artilce on Reliability and Healthy Assets. Read it for yourself here:</span></p>
<p style="line-height: 13.15pt;"><span style="font-family: 'Georgia','serif'; font-size: 9pt;"><a href="http://www.alliedreliability.com/articles/Nourishing%20Reliability%20Through%20Healthy%20Assets.pdf">&#8220;Nourishing Reliability and Healthy Assets&#8221;</a></span></p>
]]></content:encoded>
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		<slash:comments>3</slash:comments>
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		<title>Article, &#8220;uptime&#8221; Magazine: &#8220;Relieving the Tension: The Impact on Bearing Life of Overtensioned Belts&#8221;</title>
		<link>http://alliedreliabilityblog.com/2010/05/article-uptime-magazine-relieving-the-tension-the-impact-on-bearing-life-of-overtensioned-belts/</link>
		<comments>http://alliedreliabilityblog.com/2010/05/article-uptime-magazine-relieving-the-tension-the-impact-on-bearing-life-of-overtensioned-belts/#comments</comments>
		<pubDate>Fri, 07 May 2010 17:27:32 +0000</pubDate>
		<dc:creator>Allied</dc:creator>
				<category><![CDATA[Articles]]></category>
		<category><![CDATA[Asset Health]]></category>
		<category><![CDATA[Maintenance]]></category>
		<category><![CDATA[thermography]]></category>
		<category><![CDATA[vibration]]></category>
		<category><![CDATA[vibration analysis]]></category>

		<guid isPermaLink="false">http://alliedreliabilityblog.com/?p=105</guid>
		<description><![CDATA[Jeremy Davis, alongside co-author Hunter Golden, wrote an artilce on tension belts  that is featured in the February/March Edition of &#8220;uptime&#8221; Magazine. Read it for yourself here: Relieving the Tension]]></description>
			<content:encoded><![CDATA[<p></p><p style="line-height: 13.15pt;"><span style="font-family: 'Georgia','serif'; font-size: 9pt;">Jeremy Davis, alongside co-author Hunter Golden, wrote an artilce on tension belts  that is featured in the February/March Edition of &#8220;uptime&#8221; Magazine. Read it for yourself here: </span></p>
<p style="line-height: 13.15pt;"><span style="font-family: 'Georgia','serif'; font-size: 9pt;"><a title="Relieving the Tension" href="http://www.nxtbook.com/nxtbooks/reliabilityweb/uptime_20100203/#/46">Relieving the Tension</a></span></p>
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		<slash:comments>3</slash:comments>
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		<title>Vibration Readings On Compressor</title>
		<link>http://alliedreliabilityblog.com/2009/10/vibration-readings-on-compressor/</link>
		<comments>http://alliedreliabilityblog.com/2009/10/vibration-readings-on-compressor/#comments</comments>
		<pubDate>Mon, 12 Oct 2009 22:57:20 +0000</pubDate>
		<dc:creator>Allied</dc:creator>
				<category><![CDATA[Asset Health]]></category>
		<category><![CDATA[Case Study]]></category>
		<category><![CDATA[Maintenance]]></category>
		<category><![CDATA[compressor]]></category>
		<category><![CDATA[machine parts]]></category>
		<category><![CDATA[motor]]></category>
		<category><![CDATA[vibration]]></category>
		<category><![CDATA[vibration analysis]]></category>

		<guid isPermaLink="false">http://alliedreliabilityblog.com/?p=69</guid>
		<description><![CDATA[SUBMITTED BY: John H. Williams TITLE: Vibration Analyst EQUIPMENT: 700 HP Frick ammonia compressors. TECHNOLOGIES APPLIED: Vibration analysis and Ultrasound. PROBLEM DESCRIPTION: Vibration readings came into alarm on #6 Frick ammonia high stage compressor. Vibration readings taken on the outboard side of the male and female compressor screw bearings continued to rise. Readings went into [...]]]></description>
			<content:encoded><![CDATA[<p></p><p><strong>SUBMITTED BY</strong><strong>:</strong> John H. Williams</p>
<p><strong>TITLE</strong>: Vibration Analyst</p>
<p><strong>EQUIPMENT:</strong> 700 HP Frick ammonia compressors.</p>
<p><strong>TECHNOLOGIES APPLIED</strong>:<br />
Vibration analysis and Ultrasound.</p>
<p><strong>PROBLEM DESCRIPTION</strong><strong>:</strong></p>
<p>Vibration readings came into alarm on #6 Frick ammonia high stage compressor. Vibration readings taken on the outboard side of the male and female compressor screw bearings continued to rise. Readings went into alarm in April. Work order was written to repair compressor. Work was submitted for approval. Unit was shut down until work was completed.</p>
<p><strong>INVESTIGATION:</strong></p>
<p><img style="margin-left: 0px; margin-right: 0px;" src="http://www.alliedreliability.com/images/clip_image002_0006.jpg" alt="" hspace="0" /><strong> </strong></p>
<p>Base line reading on male screw conveyor 12/14/2005</p>
<p><strong><img src="http://www.alliedreliability.com/images/clip_image004_0003.jpg" alt="" /></strong><strong> </strong></p>
<p>Readings into alarm on 4/14/2006<strong> </strong></p>
<p><img src="http://www.alliedreliability.com/images/clip_image006_0002.jpg" alt="" /></p>
<p>Readings after repairs 11/6/06</p>
<p><strong>CONCLUSION:</strong><strong> </strong>Compressor refurbished and bearings replaced. New readings were taken above. The unit was able to be repaired in place with significant costs savings versus sending compressor out for repairs. Problem was located before any damage happened to screws or compressor head. Bearings were found to have significant wear after 10 years of running time and poly metallic bearing cages had broken down. A spacer for the thrust bearings was found to be in backwards also<strong>. </strong></p>
<p><strong>Thrust Bearing                                  Bearing Cage Gone </strong></p>
<div>
<table border="0" cellspacing="6" cellpadding="0" width="248">
<tbody>
<tr>
<td align="left" valign="top"><img src="http://www.alliedreliability.com/images/clip_image008_0000.jpg" alt="" /></td>
<td align="left" valign="top"><img src="http://www.alliedreliability.com/images/clip_image010_0000.jpg" alt="" /></td>
</tr>
</tbody>
</table>
</div>
<p><strong>IN SUMMARY</strong><strong>:</strong></p>
<p>When suspect readings show up, you can check bearings for cage failure by shutting down the compressor and turning machine coupling over by hand. Listen with mechanic’s stethoscope and you should hear the rollers hitting as the shaft turns over. The bearing cage is usually the first thing to fail on these compressors<strong>. </strong></p>
<p>It’s much better to locate the problem now before catastrophic failure.</p>
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		<title>Carbon Furnace Induced Draft Fan</title>
		<link>http://alliedreliabilityblog.com/2009/10/carbon-furnace-induced-draft-fan/</link>
		<comments>http://alliedreliabilityblog.com/2009/10/carbon-furnace-induced-draft-fan/#comments</comments>
		<pubDate>Mon, 12 Oct 2009 22:49:12 +0000</pubDate>
		<dc:creator>Allied</dc:creator>
				<category><![CDATA[Asset Health]]></category>
		<category><![CDATA[Case Study]]></category>
		<category><![CDATA[Maintenance]]></category>
		<category><![CDATA[spectrum reading]]></category>
		<category><![CDATA[vibration]]></category>
		<category><![CDATA[vibration analysis]]></category>

		<guid isPermaLink="false">http://alliedreliabilityblog.com/?p=66</guid>
		<description><![CDATA[SUBMITTED BY: Jamie Duart TITLE: Level III Vibration Analyst EQUIPMENT: Carbon Furnace Draft Fan TECHNOOGIES APPLIED:  Vibration PROBLEM DESCRIPTION: The Carbon Furnace Induced Draft Fan is an overhung, radial blade fan mounted on top of the carbon furnace. It is a direct-drive, variable speed application. Vibration amplitudes vary greatly from month to month and overall [...]]]></description>
			<content:encoded><![CDATA[<p></p><p><strong>SUBMITTED BY:</strong> Jamie Duart</p>
<p><strong>TITLE:</strong> Level III Vibration Analyst</p>
<p><strong>EQUIPMENT: </strong>Carbon Furnace Draft Fan</p>
<p><strong>TECHNOOGIES APPLIED:  </strong>Vibration</p>
<p><img src="http://www.alliedreliability.com/images/clip_image002_0005.jpg" alt="" /><strong><span style="text-decoration: underline;"> </span></strong></p>
<p><strong>PROBLEM DESCRIPTION: </strong><br />
The Carbon Furnace Induced Draft Fan is an overhung, radial blade fan mounted on top of the carbon furnace. It is a direct-drive, variable speed application. Vibration amplitudes vary greatly from month to month and overall vibration is over 1 in/sec on some surveys. A long history of work orders exist in our CMMS system ranging from physical removal of fan for cleaning to bearing replacement to adding mass and stiffness.  </p>
<p><strong>INVESTIGATION:</strong></p>
<p><strong>Analysis:</strong><strong> </strong>With many variable speed applications vibration data goes in and out of alarm from survey to survey. In many cases this is a result of resonance.  Resonance is when a forcing frequency such as imbalance, misalignment, looseness, bearing defects, gear defects, etc., coincides with a natural frequency. The natural frequency may be that of the rotor itself or may be that of the support frame or foundation or even drive belts. It was suspected that the Carbon Furnace Induced Draft Fan at our facility was experiencing resonance and different testing methods were employed and much research was done to prove our theory. </p>
<p><strong>Comparative Analysis:</strong>  On the following page is a horizontal, vertical and axial view of the coupling side fan bearing on the Carbon Furnace Induced Draft Fan. The spectrums show that the readings in the horizontal direction are significantly higher than in the other two directions. One of the characteristics of resonance is that it causes much higher vibration in one direction as compared to the other tri-axial directions. When resonant, it is common for the resonant direction to be 5 to 15 times higher than in the two other directions.</p>
<p><img src="http://www.alliedreliability.com/images/clip_image004_0002.jpg" alt="" /></p>
<p><strong>Natural Frequency and Resonance Detection:</strong><strong><span style="text-decoration: underline;"> </span></strong>Component natural frequencies can be detected utilizing several different methods including Impact/Impulse Natural Frequency Testing (also referred to as a “Bump Test”) and Run-up and Coast-down Testing.  Impact Naturally Frequency Testing should be performed with the piece of equipment shutdown and could not be performed due to production schedules. A Run-up Coast-down Test was the best option in this case and we employed a technique of this test called a Bode’ Plot. This Plot consists of two different plots &#8211; one of amplitude versus RPM and the other of phase versus RPM. Past vibration history showed that the Coupling side fan bearing, horizontal position showed the most response and was the point chosen for our testing. The results of this test can be found on the next page. Data shows that the characteristic 90-degree shift and rise in vibration amplitude seen at resonance occurs at approximately 64% of these units operating speed or 1360 RPM. </p>
<p>Questions arose as to whether this resonance may have been caused by the fan being out-of-balance or misaligned. These conditions could have been the forcing frequencies that coincided with the structures natural frequency and resulted in resonance excitation. A laser alignment had been performed immediately before conducting the Run-up/Coast-down test and the assumption was made that this was not the forcing frequency responsible for the resonant condition. The phase shift that had occurred at 1360 RPM and the steady decrease in vibration as RPM was increased to 2081 RPM was uncharacteristic of an out-of-balance condition. Attempts to balance this fan would likely have been unsuccessful without changing the natural frequency of the structure. This natural frequency may be lowered by adding mass or raised by adding stiffness.</p>
<p><strong><span style="text-decoration: underline;"><img src="http://www.alliedreliability.com/images/clip_image006_0001.jpg" alt="" /><strong><span> </p>
<p></span></strong></span></strong><br />
<strong><span style="text-decoration: underline;"><img src="http://www.alliedreliability.com/images/clip_image008.jpg" alt="" /></span></strong></p>
<p><strong>Physical and Analytical Research</strong>: Closer examination of the structure confirms that support and stiffness is inadequate. Conversations with Robinson Fans (the manufacturer of this fan) stated that they recommend the foundation supporting the assembly weigh a minimum of five (5) times the weight of the assembly (motor, fan, bearings, shaft and base). In this case the assembly weighs approximately 3700 lbs. total.  Five times this amount would be an approximate value of 18,500 lbs. Since this fan sits on two I-beams mounted to the top of a furnace it is doubtful that the base approaches this value. The tank-like construction of the furnace may not be able to support a massive foundation like what is recommended. </p>
<p>The fan company representative also addressed our concerns about the A-frame base that the motor and fan bearings are mounted to not being adequate to dampen frequencies excited by the fan. He explained that the weight of the base assembly (including the motor and fan bearings) provided by Robinson was roughly ten (10) times that of the fan and should provide adequate damping (fan and shaft weight is approximately 320 lbs. and the motor, base and fan bearing weight totals approximately 3700 lbs.).</p>
<p>Another concern we had was that this fan may not have been designed for a variable speed application and that we were exceeding the fans operating speed or operating at a critical frequency of the fan. Robinson explained that they typically design their fans with a critical speed at least 40% above the maximum speed rating. Maximum speed listed on the fan curve is 2183 RPM and currently the fan does not exceed 2081 RPM.</p>
<p><strong>RECOMMENDATION:</strong><br />
After careful review of the data including vibration analysis, fan company recommendations and work order history in our CMMS system it has been determined that the best course of action would be to relocate this fan to the level above the furnace. This would allow installation of a more substantial base to change the natural frequency of the unit and eliminate the resonant condition that is occurring.</p>
<h3><strong>CONCLUSION:</strong></h3>
<p>In April of 2006 the Carbon Furnace ID Fan was moved from the top of the Carbon Furnace to a newly constructed platform on the level above. Structural I-beams were added and a concrete pad was poured. Fan vibration was checked upon startup and levels were found to have risen at 2081 RPM from approximately .25 in/sec to nearly .5 in/sec. Although vibration amplitudes had risen there was little change in phase. Phase only fluctuated about 30 degrees from 40 to 100%. Vibration amplitude did see a slight rise at about 80% but did not appear to be a resonance (characteristic phase shift was not present). Time constraints prevented completion of a precision field balance but running speed vibration was lowered to approximately .25 in/sec. Balancing was accomplished the following month with final readings of .04 in/sec at 2081 CPM.</p>
<p>Below are pictures of the new structure as well as pictures of the old location on top of the furnace.</p>
<p><strong><span style="text-decoration: underline;"><img src="http://www.alliedreliability.com/images/clip_image010.jpg" alt="" /></span></strong></p>
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